1990-11-01 WorkshopV1 lUY U1 V111UUU11U UU(j
C I T Y C O U N C I L W O R K S H O P
November 1, 1990 - 7:00 P.M.
SUMMARY OF COUNCIL DISCUSSION
PG I OF 5
COUNCILMEMBERSIAC7I0N
YES
W
J-tA&SEM
A. Call workshop to order.
Mayor Chapman called the workshop to order at 7:00 P.M.
B. Mayor and Council attendance:
Mayor Oakland R. Chapman
Present
Councilman R.R. "Nick" Collins
Present
Councilman James "Jim" Kirk
Present
Councilman Oscar Thomas
Present
Councilman Dowling R. Watford, Jr.
Present
Staff attendance:
City Attorney John R. Cook
Present
City Administrator John J. Drago
Present
City Clerk Bonnie S. Thomas
Absent
City Deputy Clerk S. Lane Earnest
Present
C. Discuss the Groundwater Feasibility Study -
Discussion of GROUNDWATER FEASIBILITY STUDY:
Engineer Bill Reese.
Engineer Reese presented the Council with afeasbility study which
included the following recommendations:
"The following recommendations are based on the findings of this
study. The recommendations are intended to be taken sequentially,
as presented. Collectively, they represent a plan for the
elimination of the existing water problems and a mechanism to
maintain treatment and pumping capabilities ahead of demands.
Obviously, changes to regulatory criteria can require a
modification to the program. After the engineer is authorized
to proceed with the design, permitting, and the construction phase
of the work, the following steps should be completed, in order:
NOVEMBER 1. 7990 - WORKSHOP MEETING
PG 2 OF 5
COUNCILMEMBERS/ACTION
VOTE
YES
NO
ABSEM
1. fye dt a consumptive use permit application for the well
r_! Discusion Continued
I
2. Prepare design, permitting and bidding documents for the
wells. The drilling and testing will be done one at a time,
so each successive well will benefit from data obtained from
the previous. This also minimizes risk exposure if a
currently unknown problem is encountered. It is probable
that data from the first test production consumptive use
permit.
3. Proceed accordingly with design, permitting, and construction
of upgrade facilities for the existing WTP. In the interest
of cost savings it may be prudent to incorporate this
construction with the new WTP construction.
4. Proceed with pilot testing of the surficial aquifer well.
This should be done during the aquifer performance test
required by SFWMD to avoid cost redundancy. If the results
of the pilot study indicate effective treatment with Mn-
Greensand, proceed with design accordingly. Otherwise,
proceed with design of a lime softening facility.
5. After all wells are drilled and full analytical testing
completed, proceed with construction of the water treatment
plant. The plant should be designed, permitted and bid while
the wells are being constructed and tested.
6. Continue contact with the power company to define beneficial
inter -relationships at it relates to water source and
treatment'capabilities.
7. In early 1993 establish a firm commitment for water with the
power company and/or, commence investigations for additional
groundwater resource to expand the existing facility.
8. Maintain a constant awareness of the need for future well
sites north of the City and secure sites with access when
feasible.
Total Preliminary Cost Estimate for Mn-Greensand Filtration Plant
$3,505,000.00
Total Preliminary Cost Estimate for Lime Softening Plant
C. Discussion Continued . . .
NOVEMBER 1, 1990 - WORKSHOP MEETING
COUNCILMEMBERS/ACTION
As per the Council's request Engineer Bill Reese of Reese, Macon
and Associates brief ly reviewed the existing water treatment plant
to give recommendations and/or modifications. Engineer Reese
recommendations are as follows with cost estimates:
1. Delete softening and use circular basin for stabilization
and/or standby settling.
"Historical records show that the water is softened infrequently
and only a limited amount when softening does occur. Further,
the existing plant configuration does not permit the delivery of
a stabilized water to both sets of filters. (The old filters
receive a very low pH water and the newer filters receive a very
high pH water). This leads to continuing problems with
filtration, high maintenance costs and difficult operation.
To further complicate this matter, lime is used for pH
stabilization in the circular basin. Overfeeding is necessary
due to plant hydraulics,, as discussed above, which yields a lime
sludge problem and inefficient chemical usage.
Abandonment of softening, and conversion of the circular basin
is recommended. Although it is prudent to maintain the lime
feeders for emergency use, conversion to 50% sodium hydroxide in
recommended for pH adjustment. Confirmatory data on the
conversion to sodium hydroxide is attached for your use."
Preliminary Estimated Total Cost - $300,000.00
2. Replace existing carbon feeder.
"The existing carbon feeder is not of adequate capacity to meet
all possible. demands and should be equipped with a bag breaker,
exhaust fan and filter. The equip[ment can be located at the same
position as the existing."
Preliminary Estimated Total Cost - $94,000.00
PG 3 OF 5
VOTE
W1
NOUFMBFR 1. 1990 - WORKSHOP MEETING
PG4OF5
COUNCILMEMBERS/ACTION
VOTE
YES
W
ASSFNf
3. New polymer feed system.
C,. Discussion Continued
"This facility should have a simplistic polymer feed system for
treatment flexibility."
Preliminary Estimated Total Cost - $2,000.00
4. New phosphate feed system.
'
"Sodium hexametaphosphate will help to polish the finish water
and impede any corrosive tendencies."
Preliminary Estimated Total Cost - $20,000.00
5. Replace existing dry alum feed with liquid.
"Converting from dry to liquid feed will have a significant impact
on operator time for loading and maintenance for the alum feeders.
In addition, the unit cost savings converting to liquid alum will
result in net chemical savings of $60,000-$70,00 per year."
�!
ti
Preliminary Estimated Total Cost - $95,000.00
6. Replace transfer pumps.
"The existing transfer pumps do not have sufficient capacity to
deliver the total plant flow with one out of service. The city
has advised that there are two new replacement pumps and motors
on -site and available for installation."
Preliminary Estimated Total Cost - $33,000.00
Following a lenghty discussion among Council and Engineer Reese
is was agreed upon to have subject as an agenda item and make
final decision at the next Council meeting. (item was on 12/04/90
agenda)
ADJOURNMENT
Mayor Chapman:
NOTICE IS HEREBY GIVEN THAT IF ANY PERSON SHOULD
DECIDE TO APPEAL ANY DECISION MADE AT THIS MEETING
OF THE CITY COUNCIL, SUCH PERSON WILL NEED TO INSURE
THAT A VERBATIM RECORD OF THE PROCEEDING IS MADE WHICH
INCLUDES THE TESTIMONY AND EVIDENCE UPON WHICH THE
APPEAL IS BASED. A COPY OF THE RECORDING CAN BE
OBTAINED IN THE CITY CLERK'S OFFICE.
&Oakland-R. C apman, ayor
Attest:
Bonnie Tlramas, City Clerk, CMC
NOVEMBER 1, 1990 - WORKSHOP MEETING PG 5 OF 5
FV�OT�E�
COUNCILMEMBERS/ACTION W
Mayor Chapman adjourned the workshop at 8:56 P.M.